Friday, September 10, 2010

BP Disaster

This article was in the Wall Street Journal May 27, 2010. Reading it one sees BP making arrogant and fatal decisions with inexperienced personal. As one who has inspected, monitored and supervised millions of dollars of work in construction reading this appalled me. It is clear that BP had no respect for it’s inspector in this case the federal government. The ineptitude and total disregard for “best practices” procedures just blows me away. When you run into a contractor like this in construction or any industry two things happen if you are a good inspector:
1. You put them on notice nothing will be tolerated. Everything is by the book. You inspect 100% of everything all the time if needed. You use the toughest standards “Best Practices” you can get away with. You make them a enemy and ride their ass all the way to the end of the project.
2. If they threaten you or someones life by their disregard for “Best Practices” or their irresponsible procedures you walk away and report it to your boss, OSHA, company lawyers, police and anyone that will listen. You refuse to continue the job. In the case of the subcontractor, Transocean, the foreman should have assumed the role of the federal inspector due to the lack of federal oversight. Good inspectors will tell foremen that they are the first line of inspection and it is in their best interest to get things right the first time. How tragically true that is here. The foreman should have taken his crew and walked off the job if he felt his crew was in danger. Maybe he would have been fired but 11 people would be alive today. No job is worth your life. A lesson learned the hard way on Well No. 60-817-44169.
This is another example of why its best for private industry to regulate itself. Without federal oversight and overconfidence this disaster never would have occurred. The federal governments lax oversight set the stage for this total disregard for safe operation practices.

By BEN CASSELMAN And RUSSELL GOLD
It was a difficult drill from the start.
API Well No. 60-817-44169 threw up many challenges to its principal owner, BP PLC, swallowing expensive drilling fluid and burping out dangerous gas. Those woes put the Gulf of Mexico project over budget and behind schedule by April 20, the day the well erupted, destroying the Deepwater Horizon rig and killing 11 men.

BP Disaster


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Government investigators have yet to announce conclusions about what went wrong that day. The final step in the causation chain, industry engineers have said in interviews, was most likely the failure of a crucial seal at the top of the well or a cement plug at the bottom.
But neither scenario explains the whole story. A Wall Street Journal investigation provides the most complete account so far of the fateful decisions that preceded the blast. BP made choices over the course of the project that rendered this well more vulnerable to the blowout, which unleashed a spew of crude oil that engineers are struggling to stanch.
BP, for instance, cut short a procedure involving drilling fluid that is designed to detect gas in the well and remove it before it becomes a problem, according to documents belonging to BP and to the drilling rig’s owner and operator, Transocean Ltd.
BP also skipped a quality test of the cement around the pipe—another buffer against gas—despite what BP now says were signs of problems with the cement job and despite a warning from cement contractor Halliburton Co.
Once gas was rising, the design and procedures BP had chosen for the well likely gave this perilous gas an easier path up and out, say well-control experts. There was little keeping the gas from rushing up to the surface after workers, pushing to finish the job, removed a critical safeguard, the heavy drilling fluid known as “mud.” BP has admitted a possible “fundamental mistake” in concluding that it was safe to proceed with mud removal, according to a memo from two Congressmen released Tuesday night.
More on the Spill
See graphics covering how the spill happened, what’s being done to stop it, and the impact on the region.
Finally, a BP manager overseeing final well tests apparently had scant experience in deep-water drilling. He told investigators he was on the rig to “learn about deep water,” according to notes of an interview with him seen by the Journal.
Some of these decisions were approved by the U.S. Interior Department’s Minerals Management Service, which has come under fire for what President Obama has called its “cozy relationship” with the oil industry. But in at least one case, the decision made apparently diverged from a plan MMS approved. MMS declined to comment.
Some of BP’s choices allowed it to minimize costly delays. “We were behind schedule already,” said Tyrone Benton, a technician who operated underwater robots and worked for a subcontractor. He said that on the day before the accident, a Monday, managers “hoped we’d be finished by that Friday…. But it seemed like they were pushing to finish it before Friday.”
He added: “They were doing too many jobs at one time.” Mr. Benton is suing BP and Transocean claiming physical injury and mental anguish.
Photos: The Gulf Coast
BP acknowledges the well was running over budget but says it didn’t cut corners. “Safe and reliable operations remain a priority regardless of how much a well is behind schedule or over budget,” spokesman Andrew Gowers wrote in an email.
Some workers agree safety was paramount for both BP and Transocean. “Safety was their No. 1 concern. Protecting the environment was their No. 1 concern,” said Darin Rupinski, a Transocean employee whose job was to help keep the rig in place.
BP was drilling to tap an oil reservoir it had identified called Macondo, the same name as the cursed town in Gabriel Garcia Marquez’s novel “One Hundred Years of Solitude.” As on many past projects, BP hired a drilling rig from Transocean, the largest deep-water driller. Workers from Transocean and other contractors did most of the work, under the supervision of BP employees on the rig and in Houston.
BP started working on the well in October, using a different rig. After three weeks natural gas got into the well, called a “kick.” That’s not uncommon. But two weeks later a hurricane damaged the rig and it had to be towed to port for repairs.
BP started again in January, this time with Transocean’s Deepwater Horizon, a warhorse rig that had worked for BP for years. BP filed a new drilling permit with federal regulators.
According to a company document seen by the Journal, BP approved spending $96.2 million and about 78 days on the well. The target time was much less—about 51 days. By April 20, the well was in its 80th day, owing to delays such as one that had begun on March 8.
That day, workers discovered that gas was seeping into the well, according to drilling reports from the rig reviewed by the Journal. Workers lowered a measuring device to determine what was happening, but when they tried to pull it back up, it wouldn’t budge. Engineers eventually told them to plug the last 2,000 feet of the then-13,000-foot hole with cement and continue the well by drilling off in a different direction.
The episode took days to resolve, according to drilling reports, not counting time lost to backtracking and re-drilling. Each additional day cost BP $1 million in rig lease and contractor fees.
Other problems arose. The rock was so brittle in places that drilling mud cracked it open and escaped. One person familiar with the matter estimates BP lost at least $15 million worth of the fluid.
More
* Graphic: Likely Cause of the Deepwater Disaster
* ‘Top Kill’ Operation Under Way
* Opinion: Advice for BP’s Reputation Crisis
* BP Aims to Avoid Fresh Limits on Drilling
* Vote: What should liability cap be for oil firms?
* Insurers Caught in the Tide
* Topics: The Deepwater Oil Spill
Still, by mid-April, the well seemed a qualified success. BP was convinced it had found a lot of oil. Until engineers in Houston could make plans to start pumping it out, the workers on the nearly complete well, in a standard practice, would plug it and temporarily abandon it.
One of the final tasks was to cement in place the steel pipe that ran into the oil reservoir. The cement would fill the space between the outside of the pipe and the rock, preventing any gas from flowing up the sides.
Halliburton, the cementing contractor, advised BP to install numerous devices to make sure the pipe was centered in the well before pumping cement, according to Halliburton documents, provided to congressional investigators and seen by the Journal. Otherwise, the cement might develop small channels that gas could squeeze through.
In an April 18 report to BP, Halliburton warned that if BP didn’t use more centering devices, the well would likely have “a SEVERE gas flow problem.” Still, BP decided to install fewer of the devices than Halliburton recommended—six instead of 21.
BP said it’s still investigating how cementing was done. Halliburton said that it followed BP’s instructions, and that while some “were not consistent with industry best practices,” they were “within acceptable industry standards.”
The cement job was especially important on this well because of a BP design choice that some petroleum engineers call unusual. BP ran a single long pipe, made up of sections screwed together, all the way from the sea floor to the oil reservoir.
‘They were doing too many jobs at one time,’ says Tyrone Benton, who worked on the rig.
Companies often use two pipes, one inside another, sealed together, with the smaller one sticking into the oil reservoir. With this system, if gas tries to get up the outside of the pipe, it has to break through not just cement but also the seal connecting the pipes. So the more typical design provides an extra level of protection, but also requires another long, expensive piece of pipe.
“I couldn’t understand why they would run a long string,” meaning a single pipe, said David Pursell, a petroleum engineer and managing director of Tudor, Pickering, Holt & Co., an energy-focused investment bank. Oil major Royal Dutch Shell PLC, in a letter to the MMS, said it “generally does not” use a single pipe.
BP’s Mr. Gowers said the well design wasn’t unusual. BP engineers “evaluate various factors” to determine what design to use for each well, he said.
Despite the well design and the importance of the cement, daily drilling reports show that BP didn’t run a critical, but time-consuming, procedure that might have allowed the company to detect and remove gas building up in the well.
Before doing a cement job on a well, common industry practice is to circulate the drilling mud through the well, bringing the mud at the bottom all the way up to the drilling rig.
This procedure, known as “bottoms up,” lets workers check the mud to see if it is absorbing gas leaking in. If so, they can clean the gas out of the mud before putting it back down into the well to maintain the pressure. The American Petroleum Institute says it is “common cementing best practice” to circulate the mud at least once.
Circulating all the mud in a well of 18,360 feet, as this one was, takes six to 12 hours, say people who’ve run the procedure. But mud circulation on this well was done for just 30 minutes on April 19, drilling logs say, not nearly long enough to bring mud to the surface.
Darin Rupinski, also aboard when Deepwater Horizon exploded, has a different view: ‘Safety was their No. 1 concern.’
This decision could have left gas at the bottom of the well. When workers poured in cement to seal the sides, that gas would have been pushed up the outside of the well. Expanding as it rose, it would have reached the top of the well, where it either would have pushed against a massive seal on the ocean floor or might have gone even higher and reached the bottom of the pipe connecting the well to the drilling rig.
BP’s Mr. Gowers said the amount of time spent circulating mud is “one of many parameters considered when designing a successful cement job.” He said BP’s investigation is ongoing.
Three offshore engineers the Journal asked to review the drilling reports all pointed to the failure to circulate the mud completely as a serious mistake. Robert MacKenzie, a former oil-industry cementing engineer now at FBR Capital Markets, said, “If you have any worries about gas, if you have any worries about getting a good cement job, you should definitely do it.”
BP also didn’t run tests to check on the last of the cement after it was pumped into the well, despite the importance of cement to this well design and despite Halliburton’s warning that the cement might not seal properly. Workers from Schlumberger Ltd. were aboard and available to do such tests, but on the morning of April 20, about 12 hours before the blowout, BP told Schlumberger workers their work was done, according to Schlumberger. They caught a helicopter back to shore at 11 a.m.
BP told the Journal Tuesday that the tests weren’t run because they were needed only if there were signs of trouble in the cement job, and the work seemed to go smoothly. But the same day, BP officials told congressional investigators there were signs before the disaster that the cement might have been contaminated and that some cementing equipment didn’t work properly, according to a memo from two Congressmen.
The mood aboard the rig on April 20 was upbeat. The work was nearly done, and workers were eager to put the troublesome well behind them.
Some saw indications that managers wanted to wrap up quickly. Kevin Senegal, a subcontractor employee who cleaned tanks, said he was told to be ready to clean two tanks on a coming shift instead of the usual one. “To me it looked like they were trying to rush everything,” he said.
Drilling “mud,” perhaps mixed with oil, appeared to spew from BP’s crippled well Wednesday, the company said, after workers began trying to plug it. CEO Tony Hayward said success wouldn’t be clear until Thursday.
A disagreement broke out on the rig on April 20 over the procedures to be followed. At 11 a.m., workers for the half-dozen contractors working on the rig gathered for a meeting. Douglas Brown, Transocean’s chief mechanic on the rig, testified Wednesday at a hearing in Louisiana that a top BP official had a “skirmish” with top Transocean officials.
The Transocean workers, including offshore installation manager Jimmy Wayne Harrell, disagreed with a decision by BP’s top manager about how to remove drilling mud and replace it with lighter seawater. Mr. Brown said he heard Mr. Harrell say, “I guess that is what we have those pinchers for,” referring to a part of the blowout preventer that would shut off the well in case of an emergency.
BP won the argument, said Mr. Brown, who is a plaintiff in a suit against BP and Transocean. Mr. Harrell declined Journal requests for comment.
A little after 5 p.m., to check the well’s integrity and whether gas was seeping in, rig workers did what is called a “negative pressure test.” It was supervised by a BP well-site leader, Robert Kaluza. His experience was largely in land drilling, and he told investigators he was on the rig to “learn about deep water,” according to Coast Guard notes of an interview with him. BP declined to comment on his experience.
A lawyer for Mr. Kaluza said he “did no wrong on the Deepwater Horizon.”
The test initially strayed from the procedure spelled out in BP’s permit, approved by the MMS, according to the Coast Guard interview with Mr. Kaluza. When the first test results indicated something might be leaking, workers repeated the test, this time following the permitted procedure. The second time, pressure rose sharply, with witnesses saying that the well “continued to flow and spurted,” according to notes gathered by BP’s investigators that were reviewed by the Journal. BP denies violating its MMS permit.
Well-control experts say it’s clear gas was leaking into the well, most likely through the seal at the top but possibly through the bottom or even through a collapsed pipe.
Earlier this month, BP lawyers told Congress the test results were “inconclusive” or “not satisfactory.” On Tuesday, according to the Congressmen’s memo, BP said it saw signs of “a very large abnormality.”
Just two things then stood between the rig and an explosive mixture of gas and oil. One was the heavy drilling mud. The other was the blowout preventer near the sea floor. But the BOP had various problems, among them some leaking hydraulics.
By 8 p.m., BP was satisfied with the test and had enough confidence to proceed. It was this that may have been “a fundamental mistake,” a BP official told congressional staffers Tuesday, according to the memo from two members of Congress.
Following BP’s instruction, Transocean workers turned to replacing the mud with seawater, according to Coast Guard interviews with Mr. Kaluza and Donald Vidrine, the top BP official on the rig. Removing the mud keeps it from polluting the sea but also means there’s less weight to hold down any gas.
BP’s plans for the well, approved by the MMS on April 16, called for workers to remove the mud before performing two procedures designed to make sure gas couldn’t get into the well.
The first called for installing a giant spring to lock the seal at the top of the well in place after removal of the mud. There’s no evidence in rig-activity logs the spring was ever installed. If gas was coming up the sides of the well, pushing against the seal, this spring would have helped prevent leakage.
Second, BP opted to remove the mud before placing a final cement plug inside the well.
Animated footage of the “top kill” procedure which BP will perform later this week at the Deepwater Horizon site in an effort to stop the leak.
In documents presented to Congress, BP has hypothesized that gas could have gotten into the inside of the pipe through a failure of the cement at the bottom of the well. BP was planning to set a second, backup cement plug in the well before declaring its work done.
But workers began removing mud before setting this plug, leaving little to prevent any gas inside the pipe from rising to the rig. That plan was approved by the MMS on April 16, according to the permit reviewed by the Journal.
A spokeswoman for the Interior Department, of which the MMS is a part, said it was “looking at everything, from what happened on the rig that night and the equipment that was being used to the safety, testing and backup procedures.”
About 9:45, the seawater and remaining mud began to head back up the pipe. Witnesses say they saw mud shooting out of the derrick like water from a firehose. A worker on the rig floor made a frantic call to BP’s Mr. Vidrine, who had gone to his office, according to his interview with the Coast Guard.
Transocean workers raced to tame the well. Nothing worked. This was no ordinary gas kick. It was far more ferocious.
Workers rushed to hit the emergency button to activate the blowout preventer’s clamps and detach the rig from the well, according to witness accounts. They were too late. Gas flowing out found an ignition source, and an explosion rocked the rig.
Well No. 60-817-44169 was beyond control and on its way to becoming infamous.
—Vanessa O’Connell, Jeffrey Ball, Douglas A. Blackmon, Ana Campoy, Miguel Bustillo and Jennifer Levitz contributed to this article.

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